Loading...
CR 92-233 Approve Change Order Knollwood Street __n _,__ It \ y 0 I \ (; '" .' m ..y '" . November 12, 1992 o P K \ ~ Council Report 92-233 APPROVE CHANGE ORDER NO. 3 KNOLLWOOD STREET RECONSTRUCTION Proposed Action. Staff recommends adoption of the following motion: Move that Council authorize Chanqe Order No. 3 as it concerns the Knollwood street Reconstruction project. Overview Council in previous action has approved two other change orders that have come about mainly because of poor subgrade soils at the Knollwood site. This report outlines the need for a third and last order. Primary Issues to Consider 0 What is the justification for a change order? Most items under "Additions" relate to extra utility trench and street subgrade work necessary because of unsuitable soils. Previous analyses for Change Orders 1 and 2 discussed in detail the soil conditions and the various special methods and materials to address the . substandard conditions. The items in this change order fall into the same category. The additional item for pond excavation is one that came about from a resident by way of a private petition. 0 What are the costs and sources of funding? The net total change order is an addition of $55,224.30. The sources of funding are the utility funds, general revenue funds through PIR, contractual contingency funds, and assessments. 0 staff recommendation staff concurs with RLK Associates' assessment and recommends Council authorization of this change order. supporting Information 0 Change Order No. 3 0 supporting letter from RLK Associates .lo.."""G.'? Ge.,:::>~\Q. / ___ ~ . James Gessele Engineering Superintendent ... . CHANGE ORDER NO.3 RLK Associates, Ltd. 922 Mainstreet Hopkins, MN 55343 Date: November 3, 1992 TO: Widmer, Inc. Project No. & Desc. P.O. Box 219 90-0 1 St. Bonifacius, MN 55375 Knollwood Neighborhood Contract Date: June to, 1992 CONTRACT FOR: UTILITIES AND ROADWAY ---........-.......-------------------------------------------------------...---....-------------------------- You are hereby directed to make the following changes to the above mentioned contract: ADDITIONS: Unit Qu,. Unit Price Total Price Trench Backfill Sand TON 1,447.35 $ 9.70 $ 14,039.30 Common Excavation C.Y. 1,300.00 5.25 6,825.00 Haul - Back & re-stacking 1.5. 1.00 780.00 780.00 . charges, 6" D.I.P. warermain Remove brick pillars EACH 11.00 150.00 1,650.00 Select Granular Borrow, Mod.(CV)* C.Y. 1,000.00 8.10 8,100.00 6" Aggregate Base, CL 5 S.Y. 25,000.00 2.55 63,750.00 12" PVC Storm Pipe L.F. 100.00 20,00 2,000.00 Special Pond Excavation c.y. 2,800.00 7.35 20,580,00 Subtotal Additions $ 117,724.30 DEDUCTIONS 6" Aggregate Base, CI. 5 S.y, 25,000.00 2.50 (62,500.00) Subtotal Deductions $ (62,500.00) TOTAL CHANGE ORDER $ 55,22430 . . . e CHANGE ORDER NO.3' (CONTINUED) CONTRACT STATUS PER THIS CHANGE ORDER ACCEPTANCE ----------------------------------~---------------------------------------------------------------- The time to complete the contract is ENGINEER: I 'f" I RLK ASS IATES, LTD. 1 I Unchanged I I I I Increased by Days /./.: I I ~~A-~ 1 I Decreased by Days By Date The date of completion is Now OWNER: Original Contract Sum $ 661,435.50 CITY OF HOPKINS Net Change Order By By Previous Change Orders $ 114,432.93 Date Contract Sum . Prior to this Change Order $ 775,868.43 CONTRACTOR: I X I By~4?J?~ I I Addition ;..- . I I Date /1- ~ -q'-z:-- - I I Deduction Made by this change order $ 55,224.30 New Contract Sum $ 831,092.73 . [I!~~ 922 Mainstreet Hopkins, Mn. 55343 (612) 933-0972 fax: (612) 933-1153 November 6, 1992 Mr. Jim Gessele City of Hopkins 10 10 South First Street Hopkins, MN 55343 Re: Knollwood Neighborhood Project Change Order No, 3 Dear Jim: This letter is to explain the need for the items in Change Order No. 3 submitted to you on November 3, 1992. Under "Additions", Trench Backfill Sand was used to replace unsuitable soils taken from utility trenches for the last of the utility work. Additional Common Excavation was necessary due to the increase in depth for Class 5 aggregate base, from 6" to 12" in many street segments. The increase in unit price from $4,75/c.y. to $5.25/c.y. is due to the additional excavation in excess . of contract quantities which must be hauled off the site. Haul-back and re-stocking charges are for the 553 feet of 6" watermain which was deleted under Change Order No.2. Removal of brick pillars was for work in connection with the Drainage Easement on 122 Wilshire Walk. Additional Select Granular Borrow Modified, was for backfilling sub cuts as in Change Order No.2. The item for 6" Aggregate Base Class 5, was due to an increase in Contract Unit Price from $2. SOle. y'. to $2.55/c. y. This increase is due to higher placement costs caused by using Geotextile Fabric under the Class 5. which changes the method of dumping and spreading the material. The deduction item for 25,000 square yards of Class 5 at $2.50/s.y. will delete the amount of $62,500 paid in Payment No.4 under the old unit price. The item for 12" PVC Storm Pipe is for work done on the Drainage Easement on 122 Wjlshire Walk. The item for Special Pond Excavation of 2800 c.y. is for work done by request of the City to improve water quality and increase sediment storage capacity fOf the existing pond at Wilshire and Valley Way. . . Civil EngIneering · Transportation · Infrastructure Redevelopment · Landscape Architecture · Construction Management . . Mr. Jim Gessele November 6, 1992 Page 2 If you have any questions about this or future cost matters, please call. Sincerely, RLKE?:aJJ Paul D. Kroehnert, P.E. PDK:js cc: Chuck Poppler Dick Koppy Fritz Widmer . .